Commit graph

18 commits

Author SHA1 Message Date
0a09c4b785
smaller wheels 2025-12-12 12:08:50 -05:00
2aa25f49d2
floundering 2025-12-10 18:22:03 -05:00
7e6ba786eb
tuning 2025-12-10 16:24:44 -05:00
fb1667b1e2
goes and turns around 2025-12-10 14:43:01 -05:00
95c821664c
flip left and right motors (right motor has a lot of backlash) 2025-12-10 13:59:05 -05:00
60ce321906
continue until timeout 2025-12-10 13:22:34 -05:00
0ef16df511
distances currently off by PI/2, unknown why 2025-12-10 12:37:32 -05:00
356b1081f4
don't forget accumulated position error 2025-12-10 12:27:06 -05:00
0b0a656bf3
basic position PI tuning 2025-12-10 12:09:07 -05:00
a1b4dfce79
position PI loop 2025-12-10 12:00:13 -05:00
5bc480eaab
full sequence (no tuning or position feedback) 2025-12-10 01:51:47 -05:00
0fc7ba0f11
attempt to achieve left-right parity (very different) 2025-12-10 01:47:27 -05:00
9d45a49d75
tuned pid for movment while on jacks 2025-12-10 01:12:59 -05:00
e7979208b6
feedforward tuning first round 2025-12-10 00:59:56 -05:00
bf0c0b8d98
untested feedforward impl 2025-12-09 23:38:18 -05:00
cc4d99c218
tuning attempts
currently the right motor is acting funny
2025-12-06 16:27:21 -05:00
7bcd6e5f64
mended units 2025-12-06 15:36:25 -05:00
a29c852daa
factored out constants 2025-12-06 14:51:03 -05:00